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NTSB Identification: ATL01LA053
Accident occurred Tuesday, May 15, 2001 at Fort Lauderdale, FL
Aircraft: Cessna P337H, registration: N1013V
Injuries: 2 Minor
On May 15, 2001, at 1337 eastern daylight time, a Cessna P337H,
N1013V, collided with the ground 1/2 mile west of Fort Lauderdale
Executive Airport in Fort Lauderdale, Florida. The local flight
was operated by the pilot under the provisions of Title 14 CFR Part
91 with no flight plan filed. Visual meteorological conditions prevailed
at the time of the accident. The airplane sustained substantial
damage. The air transport pilot and passenger both received minor
injuries. The flight departed Fort Lauderdale Executive Airport
in Fort Lauderdale, Florida, at 1207 eastern daylight time.
Reportedly, the pilot was conducting multiple approaches and landings.
During the accident approach and landing, both engines lost power
and the pilot initiated emergency procedures. During the emergency
approach and landing, the airplane hit the middle marker beacon
that is 1/2 mile west of the airport. Then the airplane impacted
the ground, collided with a chain link fence, skidded across the
south lane of NW 31st Avenue, through the medium, across the north
lane of NW 31st Avenue and came to a stop on the chain link fence.
Examination of the airplane showed the left wing tank was dry. Approximately
4.5 gallons of aviation fuel were recovered from the right wing
tank. No noticeable fuel leaks were on the ground. Post accident
investigation and engine run-up revealed no mechanical malfunction.
The pilot was advised by the Fixed Base Operator Line Personnel
that the airplane had only 38 gallons of total fuel on board. The
pilot elected to fly without fueling up. The pilot told line personnel
that the airplane had enough fuel for his 45 minute flight. Approximately
one hour and 45 minutes later, the line personnel noticed that the
airplane was down on the west side of the airport. According to
Cessna, dual engine stoppage is possible if fuel is allowed to drop
below 8.3 gallons. The pilot did not report any mechanical problems
with the engines.
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